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Space Transportation System (STS)-133/External Tank (ET)-137 Intertank (IT) Stringer Cracking Issue and Repair Assessment: Proximate Cause Determination and Material Characterization StudySeveral cracks were detected in stringers located beneath the foam on the External Tank (ET) following the launch scrub of Space Transportation System (STS)-133 on November 5, 2010. The stringer material was aluminum-lithium (AL-Li) 2090-T83 fabricated from sheets that were nominally 0.064 inches thick. The mechanical properties of the stringer material were known to vary between different material lots, with the stringers from ET-137 (predominately lots 620853 and 620854) having the highest yield and ultimate stresses. Subsequent testing determined that these same lots also had the lowest fracture toughness properties. The NASA Engineering and Safety Center (NESC) supported the Space Shuttle Program (SSP)-led investigation. The objective of this investigation was to develop a database of test results to provide validation for structural analysis models, independently confirm test results obtained from other investigators, and determine the proximate cause of the anomalous low fracture toughness observed in stringer lots 620853 and 620854. This document contains the outcome of the investigation.
Document ID
20110023677
Acquisition Source
Langley Research Center
Document Type
Technical Memorandum (TM)
Authors
Piascik, Robert S.
(NASA Langley Research Center Hampton, VA, United States)
Date Acquired
August 25, 2013
Publication Date
December 1, 2011
Subject Category
Space Transportation And Safety
Report/Patent Number
L-20106
NASA/TM-2011-217318
NF1676L-13970
NESC-RP-10-00680
Funding Number(s)
WBS: WBS 869021.05.07.04.12
Distribution Limits
Public
Copyright
Work of the US Gov. Public Use Permitted.
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