NASA Logo

NTRS

NTRS - NASA Technical Reports Server

Back to Results
Tone generation by rotor-downstream strut interactionA JT15D fan stage was acoustically tested in the NASA Lewis anechoic chamber as part of the joint Lewis-Langley Research Center investigation of flight simulation techniques and flight effects using the JT15D engine as a common test vehicle. Suspected rotor-downstream support strut interaction was confirmed through the use of simulated support struts which were tested at three axial rotor-strut spacings. Tests were also performed with the struts removed. Inlet boundary layer suction in conjunction with an inflow control device was also explored. The removal of the boundary layer reduced the fan fundamental tone levels suggesting that the mounting and mating of such a device to the nacelle requires careful attention. With the same inflow control device installed good acoustic agreement was shown between the engine on an outdoor test stand and the fan in the anechoic chamber.
Document ID
19830044739
Acquisition Source
Legacy CDMS
Document Type
Conference Paper
Authors
Woodward, R. P.
(NASA Lewis Research Center Cleveland, OH, United States)
Balombin, J. R.
(NASA Lewis Research Center Cleveland, OH, United States)
Date Acquired
August 11, 2013
Publication Date
April 1, 1983
Subject Category
Aircraft Propulsion And Power
Report/Patent Number
AIAA PAPER 83-0767
Meeting Information
Meeting: American Institute of Aeronautics and Astronautics, Aeroacoustics Conference
Location: Atlanta, GA
Start Date: April 11, 1983
End Date: April 13, 1983
Sponsors: American Institute of Aeronautics and Astronautics
Accession Number
83A25957
Distribution Limits
Public
Copyright
Other

Available Downloads

There are no available downloads for this record.
No Preview Available