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Ammonia arcjet engine behavior in a cyclic endurance test at 10 kWThe behavior of a 30 kWe-class ammonia arcjet operated at 10 kWe during the 707 successful cycles of an endurance test is described. The propellant flow rate was 0.170 g/s, and the measured performance was about 630 s specific impulse at an efficiency of 0.34. Data obtained indicate that the terminal voltage increased over the first 300 cycles, and then remained approximately constant for the remainder of the test, which suggests that the cathode eroded initially and then reached a stable geometry. No major changes were observed in thruster performance. The test was terminated by a series of external arcs.
Document ID
19920074439
Acquisition Source
Legacy CDMS
Document Type
Conference Paper
Authors
Polk, J. E.
(Jet Propulsion Lab., California Inst. of Tech. Pasadena, CA, United States)
Goodfellow, K. D.
(Jet Propulsion Lab., California Inst. of Tech. Pasadena, CA, United States)
Pless, L. C.
(JPL Pasadena, CA, United States)
Date Acquired
August 15, 2013
Publication Date
August 1, 1992
Subject Category
Spacecraft Propulsion And Power
Report/Patent Number
IAF PAPER 92-0612
Accession Number
92A57063
Distribution Limits
Public
Copyright
Other

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