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Elimination of High-Frequency Combustion Instability in the Fastrac Engine Thrust ChamberA series of tests were conducted to stabilize the combustion of the Fastrac engine thrust chamber. The first few stability tests resulted in unstable combustion due ineffective acoustic cavity designs. The thrust chamber exhibited unstable combustion in the first-tangential mode and its harmonics. Combustion was stabilized by increasing the volume of the acoustic cavities and by plugging the dump-cooling orifices so that the cavities were uncooled. Although the first few stability tests resulted in unstable combustion, prior and subsequent long-duration performance tests of the Fastrac thrust chamber were spontaneously stable. Stability considerations during the injector faceplate design were based on the Hewitt correlation.
Document ID
19990102622
Acquisition Source
Marshall Space Flight Center
Document Type
Reprint (Version printed in journal)
Authors
Rocker, Marvin
(NASA Marshall Space Flight Center Huntsville, AL United States)
Nesman, Tomas E.
(NASA Marshall Space Flight Center Huntsville, AL United States)
Date Acquired
August 19, 2013
Publication Date
April 19, 1999
Subject Category
Inorganic And Physical Chemistry
Distribution Limits
Public
Copyright
Other

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