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Fastrac Gas Generator TestingA rocket engine gas generator component development test was recently conducted at the Marshall Space Flight Center. This gas generator was intended to power a rocket engine turbopump by the combustion of Lox and RP-1. The testing demonstrated design requirements for start sequence, wall compatibility, performance, and stable combustion. During testing the gas generator injector was modified to improve distribution of outer wall coolant and the igniter boss was modified to investigate the use of a pyrotechnic igniter, Expected chamber pressure oscillations at longitudinal acoustic modes were measured for three different chamber lengths tested. High amplitude discrete oscillations occurred in the chamber-alone configurations when chamber acoustic modes coupled with feed-system acoustics modes. For the full gas generator configuration, which included the turbine inlet manifold simulator, high amplitude oscillations occurred only at off-design very low power levels. This testing led to a successful gas generator design for the Fastrac 60,000 lb thrust engine.
Document ID
19990105709
Acquisition Source
Marshall Space Flight Center
Document Type
Conference Paper
Authors
Nesman, Tomas E.
(NASA Marshall Space Flight Center Huntsville, AL United States)
Dennis, Jay
(NASA Marshall Space Flight Center Huntsville, AL United States)
Date Acquired
August 19, 2013
Publication Date
January 1, 1999
Subject Category
Spacecraft Propulsion And Power
Meeting Information
Meeting: Thermal and Fluids Analysis
Location: Huntsville, AL
Country: United States
Start Date: September 13, 1999
End Date: September 17, 1999
Funding Number(s)
PROJECT: RTOP 242-34-ZT
Distribution Limits
Public
Copyright
Work of the US Gov. Public Use Permitted.

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