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Operational Issues in the Development of a Cost-Effective Reusable LOX/LH2 EngineThe NASA Space Launch Initiative (SLI) was initiated in early 2001 to conduct technology development and to reduce the business and technical risk associated with developing the next-generation reusable launch system. In the field of main propulsion, two LOXLH2 rocket engine systems, the Pratt & Whitney / Aerojet Joint Venture (JV) COBRA and the Rocketdyne RS-83, were funded to develop a safe, economical, and reusable propulsion system. Given that a large-thrust reusable rocket engine program had not been started in the U.S. since 1971, with the Space Shuttle Main Engine (SSME), this provided an opportunity to build on the experience developed on the SSME system, while exploiting advances in technology that had occurred in the intervening 30 years. One facet of engine development that was identified as being especially vital in order to produce an optimal system was in the areas of operability and maintainability. In order to achieve the high levels of performance required by the Space Shuttle, the SSME system is highly complex with very tight tolerances and detailed requirements. Over the lifetime of the SSME program, the engine has required a high level of manpower to support the performance of inspections, maintenance (scheduled and unscheduled) and operations (prelaunch and post-flight). As a consequence, the labor- intensive needs of the SSME provide a significant impact to the overall cost efficiency of the Space Transportation System (STS). One of the strategic goals of the SLI is to reduce cost by requiring the engine(s) to be easier (Le. less expensive) to operate and maintain. The most effective means of accomplishing this goal is to infuse the operability and maintainability features into the engine design from the start. This paper discusses some of the operational issues relevant to a reusable LOx/LH2 main engine, and the means by which their impact is mitigated in the design phase.
Document ID
20030111910
Acquisition Source
Marshall Space Flight Center
Document Type
Conference Paper
Authors
Ballard, Richard O.
(NASA Marshall Space Flight Center Huntsville, AL, United States)
Date Acquired
September 7, 2013
Publication Date
October 10, 2003
Subject Category
Spacecraft Design, Testing And Performance
Meeting Information
Meeting: 5th International Symposium on Liquid Space Propulsion
Location: Chattanooga, TN
Country: United States
Start Date: October 27, 2003
End Date: October 30, 2003
Distribution Limits
Public
Copyright
Work of the US Gov. Public Use Permitted.
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