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TF-34 turbofan quiet engine studyA study of high bypass turbofan engines in heavily sound-suppressed nacelles based on the TF-34 engine. The four-engine noise objective was 95 PNdb at four locations typical of takeoff and landing. Three engines were studied; these had fan pressure ratios, bypass ratios, and fan tip speeds respectively of 1.48/6.5/404 m/sec (1327 ft/sec), 1.25/13/305 (1000), 1.25/13/366(1200). The bypass 13 engines had a variable pitch fan, direct- and gear-driven. Noise suppressive treatment was identified which met 95 PNdb objective except for sideline liftoff at 6.5 bypass, full power, which was 2 PNdb noisier; at 90% power, 95 PNdb was achieved.
Document ID
19720026093
Acquisition Source
Legacy CDMS
Document Type
Contractor Report (CR)
Authors
Edkins, D. P.
(General Electric Co. Lynn, MA, United States)
Hirschkron, R.
(General Electric Co. Lynn, MA, United States)
Lee, R.
(General Electric Co. Lynn, MA, United States)
Date Acquired
September 2, 2013
Publication Date
January 1, 1972
Subject Category
Propulsion Systems
Report/Patent Number
NASA-CR-120914
Accession Number
72N33743
Funding Number(s)
CONTRACT_GRANT: NAS3-14338
Distribution Limits
Public
Copyright
Work of the US Gov. Public Use Permitted.
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