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Water/glycol temperature control circuit failed in the automatic mode: Apollo 16An anomaly report concerning failure of the water/glycol temperature control circuit during the Apollo 16 flight is presented. The anomaly is described and diagrams of the system are presented. The malfunction was caused by cracked semiconductor chips in the output silicon-controlled rectifier. Surface contamination in the crack allowed the device to self-gate on and remain on, resulting in a secondary failure of the feedback capacitor.
Document ID
19730018173
Acquisition Source
Legacy CDMS
Document Type
Technical Memorandum (TM)
Date Acquired
September 2, 2013
Publication Date
November 1, 1972
Subject Category
Space Vehicles
Report/Patent Number
NASA-TM-X-69234
MSC-07598
Report Number: NASA-TM-X-69234
Report Number: MSC-07598
Accession Number
73N26900
Distribution Limits
Public
Copyright
Work of the US Gov. Public Use Permitted.
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