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Analytical investigation of solid rocket nozzle failureOn April 5, 1983, an Inertial Upper Stage (IUS) spacecraft experienced loss of control during the burn of the second of two solid rocket motors. The anomaly investigation showed the cause to be a malfunction of the solid rocket motor. This paper presents a description of the IUS system, a failure analysis summary, an account of the thermal testing and computer modeling done at Marshall Space Flight Center, a comparison of analysis results with thermal data obtained from motor static tests, and describes some of the design enhancement incorporated to prevent recurrence of the anomaly.
Document ID
19860000811
Acquisition Source
Legacy CDMS
Document Type
Technical Memorandum (TM)
Authors
Mccoy, K. E.
(NASA Marshall Space Flight Center Huntsville, AL, United States)
Hester, J.
(NASA Marshall Space Flight Center Huntsville, AL, United States)
Date Acquired
September 5, 2013
Publication Date
August 1, 1985
Subject Category
Spacecraft Propulsion And Power
Report/Patent Number
NASA-TM-86513
NAS 1.15:86513
Report Number: NASA-TM-86513
Report Number: NAS 1.15:86513
Accession Number
86N10278
Distribution Limits
Public
Copyright
Work of the US Gov. Public Use Permitted.
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