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Flight set 360H005 (STS-28) seals, volume 4The performance is assessed of the 360H005, Fifth flight, Redesigned Solid Rocket Motors (RSMR) in respect to joint sealing issues as seen from post flight inspection of the seals and sealing surfaces. The factory joint disassembly inspections have resumed for 360H005. The new factory joint grease application is in effect and now can be assessed during the disassembly process. The RSRM is illustrated consisting of capture feature field joints as is the J-joint insulation configuration. The nozzle-to-case joint design is also illustrated, which includes 100, 7/8 inch radial bolts in conjunction with a wiper O-ring and modified insulation design. The ignition system seals and a cross section of the igniter are illustrated. The configuration of all the internal nozzle joints are also shown. The postflight inspection of both motors showed the seal components to be in excellent condition except for the indentation found on the inner primary seal of the right hand inner igniter gasket, aft face. Detailed inspection results, and inspections performed by the O-ring Inspection Team are presented.
Document ID
19900018735
Acquisition Source
Legacy CDMS
Document Type
Contractor Report (CR)
Authors
Curry, Jeffrey T.
(Thiokol Corp. Brigham City, UT, United States)
Date Acquired
September 6, 2013
Publication Date
February 1, 1990
Subject Category
Mechanical Engineering
Report/Patent Number
NAS 1.26:183904
NASA-CR-183904
TWR-17544-VOL-4
Report Number: NAS 1.26:183904
Report Number: NASA-CR-183904
Report Number: TWR-17544-VOL-4
Accession Number
90N28051
Funding Number(s)
CONTRACT_GRANT: NAS8-30490
Distribution Limits
Public
Copyright
Work of the US Gov. Public Use Permitted.
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