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Supplementary Ditching Investigation of a 1/18-Scale Model of the North American B-45 AirplaneA supplementary investigation of a 1/18-scale dynamically similar model of the North American B-45 airplane was made in calm water to observe the ditching behavior and to determine the effect of further conditions of simulated damage. The behavior of the model was determined from motion-picture records, time-history deceleration records, and visual observations. It was concluded that, during a ditching, the nose-wheel doors, bomb-bay doors, under surface of the aft fuselage and lower part of the bomb-bay aft bulkhead will be torn away. When such damage occurs, the diving found in the previous tests will not occur and the airplane will porpoise during the first third of the landing run and then run smoothly. Because of the extensive damage which occurs, the fuselage aft of the pilots' compartment will fill with water very rapidly and is, therefore, an undesirable ditching station. No change in the previously recommended ditching attitude and flap setting (6 deg attitude, flaps down) is indicated by these supplementary tests.
Document ID
20050030015
Acquisition Source
Langley Research Center
Document Type
Other - NACA Research Memorandum
Authors
Fisher, Lloyd J.
(National Advisory Committee for Aeronautics. Langley Aeronautical Lab. Langley Field, VA, United States)
Thompson, William C.
(National Advisory Committee for Aeronautics. Langley Aeronautical Lab. Langley Field, VA, United States)
Date Acquired
August 22, 2013
Publication Date
January 1, 1949
Subject Category
Air Transportation And Safety
Report/Patent Number
NACA-RM-SL51C29
Report Number: NACA-RM-SL51C29
Distribution Limits
Public
Copyright
Work of the US Gov. Public Use Permitted.
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