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Causes and Mitigation of Fuel Pilot Operated Valve Pilot Seal Extrusion in Space Shuttle Orbiter Primary RCS ThrustersExtrusion of a polytetrafluoroethylene (PTFE) pilot seal located in the Space Shuttle Orbiter Primary Reaction Control Subsystem (PRCS) thruster fuel valve has been implicated in 68 ground and on-orbit fuel valve failures. A rash of six extrusion-related in-flight anomalies over a six-mission span from December 2001 to October 2002 led to heightened activity at various NASA centers, and the formation of a multidisciplinary team to solve the problem. Empirical and theoretical approaches were used. For example, thermomechanical analysis (TMA) and exposure tests showed that some extrusion is produced by thermal cycling; however, a review of thruster service histories did not reveal a strong link between thermal cycling and extrusion. Calculations showed that the amount of observed extrusion often exceeded the amount allowed by thermally-induced stress relief. Failure analysis of failed hardware also revealed the presence of fuel-oxidizer reaction product (FORP) inside the fuel valve pilot seal cavity, and differential scanning calorimetry (DSC) showed that the FORP was intimately associated with the pilot seal material. Component-level exposure tests showed that FORP of similar composition could be produced by adjacent oxidizer valve leakage in the absence of thruster firing. Specific gravity data showed that extruded fuel valve pilot seals were less dense than new pilot seals or oxidizer valve pilot seals, indicating permanent modification of the PTFE occurred during service. It is concluded that some thermally-induced extrusion is unavoidable; however, oxidizer leakage-induced extrusion is mostly avoidable and can be mitigated. Several engineering level mitigation strategies are discussed.
Document ID
20050217291
Acquisition Source
Johnson Space Center
Document Type
Preprint (Draft being sent to journal)
Authors
Waller, Jess M.
(Honeywell Technology Solutions, Inc. Las Cruces, NM, United States)
Roth, Tim E.
(Honeywell Technology Solutions, Inc. Las Cruces, NM, United States)
Saulsberry, Regor L.
(NASA Johnson Space Center Houston, TX, United States)
Haney, William A.
(Honeywell Technology Solutions, Inc. Las Cruces, NM, United States)
Kelly, Terence S
(Boeing Co. Las Cruces, NM, United States)
Forsyth, Bradley S.
(Honeywell Technology Solutions, Inc. Las Cruces, NM, United States)
Date Acquired
September 7, 2013
Publication Date
January 1, 2004
Subject Category
Spacecraft Propulsion And Power
Meeting Information
Meeting: 40th Annual AIAA/ASME/ASEE Joint Propulsion Conference and Exhibit
Location: Fort Lauderdale, FL
Country: United States
Start Date: July 11, 2004
End Date: July 14, 2004
Sponsors: American Society of Mechanical Engineers, American Society for Electrical Engineers, American Inst. of Aeronautics and Astronautics
Distribution Limits
Public
Copyright
Work of the US Gov. Public Use Permitted.
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