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JANNAF Lessons Learned Panel DiscussionThe difference between the AS-510 observed and predicted separation distance is attributed to a greater F-1 engine "tail off" impulse than that used in the separation distance prediction. . The F-1 thrust decay was normal and not appreciably different from previous (AS-505 through 509) flights. . Analysis indicates that with an S-IC stage having only four retro motors, failure of one retro motor to ignite would result in marginal separation distances and, in the 3-sigma case, re-contact of the two stages. . S-IC-11 and subsequent flight stages were equipped with eight retro motors rather than the planned four.
Document ID
20100023317
Acquisition Source
Marshall Space Flight Center
Document Type
Presentation
Authors
Richards, Steve
(Bangham Engineering, Inc. Huntsville, AL, United States)
Date Acquired
August 24, 2013
Publication Date
May 3, 2010
Subject Category
Spacecraft Propulsion And Power
Report/Patent Number
M10-0609
Report Number: M10-0609
Meeting Information
Meeting: 4th Spacecraft Propulsion Joint Subcommittee Meeting
Location: Colorado Springs, CO
Country: United States
Start Date: May 3, 2010
End Date: May 7, 2010
Sponsors: Department of the Navy, NASA Headquarters, Department of the Army, Department of the Air Force
Funding Number(s)
CONTRACT_GRANT: NNM05AB50C
Distribution Limits
Public
Copyright
Public Use Permitted.
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