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Space Shuttle Main Propulsion System Gaseous Hydrogen Flow Control Valve Poppet FailureThe presentation provides background information pertinent to the MPS GH2 Flow Control Valve Poppet failure which occurred on the Space Shuttle Endeavour during STS-126 flight. The presentation provides general MPS system operating information which is pertinent to understanding the failure causes and affects. The presentation provides additional background information on the operating environment in which the FCV functions and basic design history of the flow control valve. The presentation provides an overview of the possible flight failure modes and a brief summary of the flight rationale which was developed for this failure event. This presentation is an introductory presentation to 3 other speakers at the conference who will be speaking on M&P aspects of the investigation, non destructive inspection techniques development, and particle impact testing.
Document ID
20110003995
Acquisition Source
Kennedy Space Center
Document Type
Presentation
Authors
Zeitler, Rick
(United Space Alliance Cape Canaveral, FL, United States)
Date Acquired
August 25, 2013
Publication Date
May 10, 2010
Subject Category
Fluid Mechanics And Thermodynamics
Report/Patent Number
KSC-2010-056
Report Number: KSC-2010-056
Meeting Information
Meeting: 2010 Aircraft Airworthiness and Sustainment Conference
Location: Austin, TX
Country: United States
Start Date: May 10, 2010
End Date: May 13, 2010
Funding Number(s)
CONTRACT_GRANT: NNJ06VA01C
Distribution Limits
Public
Copyright
Public Use Permitted.
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