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Space Shuttle main engine nozzle-steerhorn dynamicsOn two occasions during the Space Shuttle main engine development, the LH2 feedline (called the steerhorn, because of its shape) failed during the cutoff transient. A dynamic test was undertaken, and an analytical model was developed and correlated to the dynamic test. Detailed models of the tube bundle were required to obtain the equivalent shell coefficients. All-shell models of the nozzle wall were found better than beam-shell models. The most difficult part of the structure to simulate was the felt-metal pad between the feedline and its mount, which introduced nonlinear stiffness and damping and led to the use of separate low amplitude and high amplitude models. The total structure was found to have 400 modes in the frequency range of interest, 0 to 500 Hz. Good test analysis correlation was obtained and a modified feedline configuration was found to demonstrate a 40% reduction of response stress from the original configuration.
Document ID
19810045035
Acquisition Source
Legacy CDMS
Document Type
Conference Proceedings
Authors
Kiefling, L.
(NASA Marshall Space Flight Center Huntsville, Ala., United States)
Date Acquired
August 11, 2013
Publication Date
January 1, 1981
Subject Category
Spacecraft Propulsion And Power
Report/Patent Number
AIAA PAPER 81-0505
Meeting Information
Meeting: Conference on Structures, Structural Dynamics and Materials
Location: Atlanta, GA
Start Date: April 6, 1981
End Date: April 8, 1981
Accession Number
81A29439
Distribution Limits
Public
Copyright
Other

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