ALS LOX/H2 subscale coaxial injector testingTests of a 40K subscale LOX/H2 coaxial LOX swirl injector conducted without injector or chamber degradation are reported. Chamber pressures ranged from 1572 to 2355 psia with overall mixture ratios from 5.04 to 6.39. The highest characteristic velocities were measured when the mixture ratio across the injector face was uniform. Scarfing of the outer row LOX posts had the largest effect on chamber heating rates. As a result of the tests, the LSI design was modified to arrange the outer row LOX posts in a circular pattern, eliminate O/F biasing and fuel film cooling, and modify the interpropellant plate to allow for larger pressure differentials during the start and cutoff transients. Testing of a 100 K LOX/H2 coaxial LOX swirl injector involved chamber pressure ranging from 700 to 2500 psia with overall mixture ratios from 3.2 to 8.8. Stable combustion was observed to a fuel temperature of 90R and characteristic velocity efficiencies were good.
Document ID
19910059415
Acquisition Source
Legacy CDMS
Document Type
Conference Paper
Authors
Dexter, Carol E. (NASA Marshall Space Flight Center Huntsville, AL, United States)
Date Acquired
August 15, 2013
Publication Date
June 1, 1991
Subject Category
Spacecraft Propulsion And Power
Report/Patent Number
AIAA PAPER 91-1871Report Number: AIAA PAPER 91-1871