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RSRM Chamber Pressure Oscillations: Transit Time Models and Unsteady CFDSpace Shuttle solid rocket motor low frequency internal pressure oscillations have been observed since early testing. The same type of oscillations also are present in the redesigned solid rocket motor (RSRM). The oscillations, which occur during RSRM burn, are predominantly at the first three motor cavity longitudinal acoustic mode frequencies. Broadband flow and combustion noise provide the energy to excite these modes at low levels throughout motor burn, however, at certain times during burn the fluctuating pressure amplitude increases significantly. The increased fluctuations at these times suggests an additional excitation mechanism. The RSRM has inhibitors on the propellant forward facing surface of each motor segment. The inhibitors are in a slot at the segment field joints to prevent burning at that surface. The aft facing segment surface at a field joint slot burns and forms a cavity of time varying size. Initially the inhibitor is recessed in the field joint cavity. As propellant burns away the inhibitor begins to protrude into the bore flow. Two mechanisms (transit time models) that are considered potential pressure oscillation excitations are cavity-edge tones, and inhibitor hole-tones. Estimates of frequency variation with time of longitudinal acoustic modes, cavity edge-tones, and hole-tones compare favorably with frequencies measured during motor hot firing. It is believed that the highest oscillation amplitudes occur when vortex shedding frequencies coincide with motor longitudinal acoustic modes. A time accurate computational fluid dynamic (CFD) analysis was made to replicate the observations from motor firings and to observe the transit time mechanisms in detail. FDNS is the flow solver used to detail the time varying aspects of the flow. The fluid is approximated as a single-phase ideal gas. The CFD model was an axisymmetric representation of the RSRM at 80 seconds into burn.Deformation of the inhibitors by the internal flow was determined through an iterative structural and CFD analysis. The analysis domain ended just upstream of the nozzle throat. This is an acoustic boundary condition that caused the motor to behave as a closed-open organ pipe. This differs from the RSRM which behaves like a closed-closed organ pipe. The unsteady CFD solution shows RSRM chamber pressure oscillations predominately at the longitudinal acoustic mode frequencies of a closed-open organ pipe. Vortex shedding in the joint cavities and at the inhibitors contribute disturbances to the flow at the second longitudinal acoustic mode frequency. Further studies are planned using an analysis domain that extends downstream of the nozzle throat.
Document ID
19960029274
Acquisition Source
Marshall Space Flight Center
Document Type
Conference Paper
Authors
Nesman, Tom
(NASA Marshall Space Flight Center Huntsville, AL United States)
Stewart, Eric
(NASA Marshall Space Flight Center Huntsville, AL United States)
Date Acquired
September 6, 2013
Publication Date
March 1, 1996
Publication Information
Publication: Thirteenth Workshop for Computational Fluid Dynamic Applications in Rocket Propulsion and Launch Vehicle Technology
Subject Category
Fluid Mechanics And Heat Transfer
Accession Number
96N29770
Distribution Limits
Public
Copyright
Work of the US Gov. Public Use Permitted.
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