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Design, Development, and Integration of A Space Shuttle Orbiter Bay 13 Payload CarrierBay 13 of the Space Shuttle Orbiter has been limited to small sidewall mounted payloads and ballast. In order to efficiently utilize this space, a concept was developed for a cross-bay cargo carrier to mount Orbital Replacement Units (ORU's) for delivery to the International Space Station and provide additional opportunities for science payloads, while meeting the Orbiter ballast requirements. The Lightweight Multi-Purpose Experiment Support Structure (MPESS) Carrie (LMC) was developed and tested by NASA's Marshall Space Flight Center and the Boeing Company. The Multi-Purpose Experiment Support Structure (MPESS), which was developed for the Spacelab program was modified, removing the keel structure and relocating the sill trunnions to fit in Bay 13. Without the keel fitting, the LMC required a new and innovative concept for transferring Y loads into the Orbiter structure. Since there is no keel fitting available in the Bay 13 location, the design had to utilize the longeron bridge T-rail to distribute the Y loads. This concept has not previously been used in designing Shuttle payloads. A concept was developed to protect for Launch-On-Need ORU's, while providing opportunities for science payloads. Categories of potential ORU's were defined, and Get-Away Special (GAS) payloads of similar mass properties were provided by NASA's Goddard Space Flight Center. Four GAS payloads were manifest as the baseline configuration, preserving the capability to swap up to two ORU's for the corresponding science payloads, after installation into the Orbiter cargo bay at the pad, prior to closeout. Multiple configurations were considered for the analytical integration, to protect for all defined combinations of ORU's and GAS payloads. The first physical integration of the LMC war performed by Goddard Space Flight Center and Kennedy Space Center at an off-line facility at Kennedy Space Center. This paper will discuss the design challenges, structural testing, analytical and physical integration for the LMC's successful maiden flight on STS-108/ISS UF-1 mission in December 2001.
Document ID
20030000446
Acquisition Source
Marshall Space Flight Center
Document Type
Conference Paper
Authors
Spencer, Susan H.
(NASA Marshall Space Flight Center Huntsville, AL United States)
Phillips, Michael W.
(Boeing Co. United States)
Upton, Lanny
Date Acquired
August 21, 2013
Publication Date
January 1, 2002
Subject Category
Spacecraft Design, Testing And Performance
Meeting Information
Meeting: 53rd International Astronautical (IAF) Congress Space Station Utilization Conference
Location: Houston, TX
Country: United States
Start Date: October 10, 2002
End Date: October 19, 2002
Distribution Limits
Public
Copyright
Work of the US Gov. Public Use Permitted.

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