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Characterization of Low-Temperature, Co-Fired Ceramic-Manufactured Electrostatic Thruster-Closeout ReportThe goal of the project was to evaluate prototypes of an experimental thruster developed by the University of Arkansas (UA), Fayetteville, AR. The design under evaluation is a radio frequency (RF) electrostatic thruster that was fabricated using the low-temperature, co-fired ceramic (LTCC) materials and fabrication process. This materials system is analogous to printed circuit board (PCB) technology with the most significant difference being that the laminate is replaced by a ceramic material and the copper layer is replaced by printed sinterable silver paste. LTCC designs are baked after fabrication and assembled to realize an entirely monolithic structure with internal conductors, vias, and cavities. In this process, the LTCC electrostatic thruster (LTCC-ET) that is the subject of the present work becomes a monolithic ceramic thruster capable of withstanding temperatures in excess of 500 ºC. The UA and NASA Marshall Space Flight Center (MSFC) jointly performed prototype testing on the LTCC-ET under a NASA Cooperative Agreement Notice (CAN) award. The LTCC-ET was tested at MSFC in May 2018 over a 1-week period. There were two goals for the test program: (1) Testing to determine the operating parameters required to create plasma ignition in the test articles. This was explored by setting a propellant flowrate and increasing RF power until plasma ignition was observed. Testing was conducted with both argon and krypton. (2) Investigate the thrust and specific impulse (Isp) performance of the thruster as a function of propellant flowrate and grid voltage. This goal was not met during the project as technical challenges in maintaining stable plasma ignition arose due to stress and heating of the RF power feed. In summary, a prototype thruster design (consisting of three packaged units) was fabricated by UA and tested for the first time under vacuum conditions at MSFC to experimentally determine basic performance metrics and functionality. It was found that the design was not sufficiently optimized or robust enough in its initial iteration to support a significant test campaign or characterization program. It was concluded that the propellant outlet channels must be reduced in size with the flowpaths adjusted to increase propellant residence time in the thruster, and that the RF connector must be replaced with a version capable of handling higher power throughput and heating. However, even in its unoptimized form, a plasma could be produced in the LTCCET, demonstrating the efficacy of the design approach. The design is especially compelling due to its low cost to manufacture and, more importantly, its scalability of size and power throughput. Low cost and scalability are also important in that additional functionalities, such as thrust vectoring and plume charge neutralization, can be integrated into future designs with minimal additional cost. This project has matured the LTCC-ET development Technology Readiness Level (TRL) from 1 to 2. The low-cost RF plasma source portion of the LTCC device was matured from TRL 2 to 4 through the demonstration of RF plasma ignition under vacuum conditions.
Document ID
20190027344
Acquisition Source
Marshall Space Flight Center
Document Type
Technical Memorandum (TM)
Authors
Huang, P.-H. A.
(Arkansas Univ. Fayetteville, AR, United States)
Roddy, M.
(Arkansas Univ. Fayetteville, AR, United States)
Polzin, K. A.
(NASA Marshall Space Flight Center Huntsville, AL, United States)
Date Acquired
July 15, 2019
Publication Date
June 1, 2019
Subject Category
Spacecraft Propulsion And Power
Report/Patent Number
NASA/TM-2019–220136
M-1487
M19-7371
Distribution Limits
Public
Copyright
Public Use Permitted.
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