NASA Logo

NTRS

NTRS - NASA Technical Reports Server

Due to the lapse in federal government funding, NASA is not updating this website. We sincerely regret this inconvenience.

Back to Results
Advanced Gas Turbine (AGT) power-train system developmentTechnical work on the design and component testing of a 74.5 kW (100 hp) advanced automotive gas turbine is described. Selected component ceramic component design, and procurement were tested. Compressor tests of a modified rotor showed high speed performance improvement over previous rotor designs; efficiency improved by 2.5%, corrected flow by 4.6%, and pressure ratio by 11.6% at 100% speed. The aerodynamic design is completed for both the gasifier and power turbines. Ceramic (silicon carbide) gasifier rotors were spin tested to failure. Improving strengths is indicated by burst speeds and the group of five rotors failed at speeds between 104% and 116% of engine rated speed. The emission results from combustor testing showed NOx levels to be nearly one order of magnitude lower than with previous designs. A one piece ceramic exhaust duct/regenerator seal platform is designed with acceptable low stress levels.
Document ID
19830007356
Acquisition Source
Legacy CDMS
Document Type
Contractor Report (CR)
Authors
Helms, H. E.
(Detroit Diesel Allison Indianapolis, IN, United States)
Johnson, R. A.
(Detroit Diesel Allison Indianapolis, IN, United States)
Gibson, R. K.
(Detroit Diesel Allison Indianapolis, IN, United States)
Date Acquired
September 4, 2013
Publication Date
February 1, 1982
Subject Category
Mechanical Engineering
Report/Patent Number
NAS 1.26:167875
DDA-EDR-10977
DOE/NASA/0168-82/4
SAR-4
NASA-CR-167875
Report Number: NAS 1.26:167875
Report Number: DDA-EDR-10977
Report Number: DOE/NASA/0168-82/4
Report Number: SAR-4
Report Number: NASA-CR-167875
Accession Number
83N15627
Funding Number(s)
CONTRACT_GRANT: DEN3-168
Distribution Limits
Public
Copyright
Work of the US Gov. Public Use Permitted.
No Preview Available